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BP Criminals In The Gulf

The major media and rest of the country are catching on to what should have been patently obvious from the start, i.e. the discharge from the BP Deepwater Horizon catastrophe in the Mississippi Canyon offshore oilfield in the Gulf of Mexico is many factors larger than was being disclosed by either the relentlessly dishonest BP or the US government partnering with them in the disaster response. But while the public attention has been focused on the Top Kill well closure attempt and the mind numbing spill cam BP was finally forced to “allow” the public to see, hearings have been proceeding in not only Congress as covered by Emptywheel (see here and here), but also in Kenner Louisiana in front of a joint Coast Guard/MMS Federal inquiry board.

There have been startling revelations, especially out of the Kenner joint inquiry. The New Orleans Times Picayune is once again on a path to a Pulitzer for their disaster coverage and has given comprehensive coverage from Kenner and The Hill in Washington. Here are some items from the evidence set being adduced in Kenner and Congress:

The failed blowout preventer on the Deepwater Horizon oil rig had a hydraulic leak and a dead battery in one of its control pods, and testing in the hours before an April 20 explosion revealed that pressure in the well was dangerously out of whack.

While some data were being transmitted to shore for safekeeping right up until the April 20 blast, officials from Transocean, the rig owner, told Congress that the last seven hours of its data are missing and that all written logs were lost in the explosion.

Heavy drilling fluid was unconscionably replaced with lighter seawater against industry standards just prior to the blowout. Over heated objections by experts on the scene, BP management supervisors overruled drillers, and insisted on displacing the mud with seawater

The broken blow out preventer had not been inspected in over five years.

BP was in a severe economic and time crunch to finish the job quickly and were over six weeks behind schedule.

Immediately leading up to the explosion, BP used procedures that violated their own drill plan; and in spite of indications of a “very large abnormality,” kept testing until they got something they could disingenuously claim fulfilled the test.

BP management supervisors refused to run the comprehensive cement bond log test, a definitive test of the integrity of a well’s cement mandated by Federal Regulations if there are concerns with the results of negative and positive pressure Read more